石油学报 ›› 2005, Vol. 26 ›› Issue (3): 74-77.DOI: 10.7623/syxb200503016

• 油田开发 • 上一篇    下一篇

蒸汽吞吐后期近井地带储层的变化及其对油田开发效果的影响

杨春梅1,2, 陆大卫1,3, 张方礼2, 李洪奇1, 刘卫东2   

  1. 1. 中国石油大学资源与信息学院 北京 102249;
    2. 中国石油辽河油田公司 辽宁盘锦 124010;
    3. 中国石油天然气股份有限公司 北京 100011
  • 收稿日期:2004-08-26 修回日期:2004-11-25 出版日期:2005-05-25 发布日期:2010-05-21
  • 作者简介:杨春梅,女,1968,年2月生,1991年毕业于石油大学(华东),现为石油大学(北京)在读博士.E-mail:ycm_lh@sina.com

Reservoir characteristics in the near region of thermal recovery wells and their effects on development of oilfield in the later period of steam stimulation

YANG Chun1,2, LU Da1,3, ZHANG Fang2, LI Hong1, LIU Wei2   

  1. 1. Faculty of Natrual Resource and Information Technology, China University of Petroleum, Beijing 102249, China;
    2. Liaohe Oilfield Company, CNPC, Panjin 124010, China;
    3. PetroChina Company, Ltd. Beijing 100011, China
  • Received:2004-08-26 Revised:2004-11-25 Online:2005-05-25 Published:2010-05-21

摘要: 针对蒸汽吞吐超过5~6个周期之后稠油油藏开发效果明显变差的问题,以距原开发井仅13m的侧钻取心井为依据,研究了近井地带储层性质变化规律及其对开发效果的影响。结果表明:在开发后期,近井地带储层及流体性质变化较大,颗粒溶蚀破碎现象严重,超大管状孔发育;油层动用程度高,含油饱和度接近甚至低于实验室确定的残余油饱和度;存在不可逆的沥青积淀现象。近井地带储层性质的一系列变化是造成钻井液漏失、固井质量差、油层污染严重并最终导致加密调整井开发效果不佳的主要原因,近井地带存水量的增加降低了吞吐后期的热效率;高渗透性大孔道使蒸汽在储层中发生窜流;原油中的硫化物在高温蒸汽作用下所发生的脱硫反应使热采稠油管柱严重腐蚀。虽然近井地带储层性质的一系列变化会对开发效果造成不利影响,但是孔隙结构的改善及亲水性的增强对于提高采收率也具有一定的积极作用。

关键词: 蒸汽吞吐井, 侧钻取心井, 近井地带储集层, 渗透性, 沥青积淀, 提高采收率

Abstract: A sidetracked core hole with 13 meters away from original well in the pay zone was investigated. The changes of heavy oil reservoir property and their effects on production performances after five to six cycles of steam stimulation were analyzed. The result showed that in the later period of oilfield development,the characteristics of reservoir and fluid in the near region of thermal recovery well changed obviously. Rock grains were corroded seriously,and big pores were enhanced. The high-permeability wormhole appeared,and volume of clay decreased. Oil saturation was close to and lowers than the remaining oil saturation determined by water flooding test in laboratory. Bitumen was deposited in pores and could not be reversed. All changes have brought a series of problems in the process of steam stimulation development,such as sanding,leakage and loss of drilling fluid,poor quality of well cementing,casing failing,electrical anisotropy,steam channeling and low steam heat efficiency. Those factors affected the development effectiveness of infill wells and adjusting wells. Otherwise,wettability of reservoirs and improvement of pore structure would enhance heavy-oil recovery.

Key words: steam stimulation well, sidetracked core hole, reservoir in near region of thermal recovery well, permeability, bitumen deposition, enhanced oil recovery

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