石油学报 ›› 2006, Vol. 27 ›› Issue (4): 119-121.DOI: 10.7623/syxb200604027

• 石油工程 • 上一篇    下一篇

辽河油田超稠油掺活性水降粘先导性试验

尉小明, 刘喜林, 郭占文, 余五星   

  1. 中国石油辽河油田公司, 辽宁盘锦, 124010
  • 收稿日期:2005-08-15 修回日期:2006-01-23 出版日期:2006-07-25 发布日期:2010-05-21
  • 作者简介:尉小明,男,1972年4月生,2000年获浙江大学理学博士学位,2003年博士后出站,现为辽河油田公司钻采工艺研究院高级工程师,主要从事油田超稠油开采工艺的研究和科研管理工作.E-mail:weixm6666@126.com
  • 基金资助:
    中国石油天然气股份有限公司科技攻关项目(200509-01-1)"稠油气驱转换开采方式及提高吞吐效率配套技术研究"部分成果.

Pilot test for viscosity reduction of ultra-heavy oil by blending active water in Liaohe Oilfield

Wei Xiaoming, Liu Xilin, Guo zhanwen, Yu Wuxing   

  1. PetroChina Liaohe Oilfield Company, Panjin 124010, China
  • Received:2005-08-15 Revised:2006-01-23 Online:2006-07-25 Published:2010-05-21

摘要: 针对目前辽河油田超稠油井筒电加热降粘工艺存在能耗过高的问题,采用了井筒掺活性水降粘工艺.实验结果表明,该工艺具有较高的超稠油降粘率、自动破乳脱水性能以及与联合站用破乳剂良好的配伍性,解决了超稠油乳化降粘与破乳脱水之间的矛盾.在辽河油田8口超稠油井进行了掺活性水降粘工艺先导性试验,结果表明掺活性水降粘技术可以取代电加热降粘技术维持正常生产.试验油井抽油机电流下降10~30 A、井口产出液粘度大大下降.采用污水回掺工艺流程实现了污水循环往复使用,节约了大量的清水资源.采用掺活性水降粘技术后原油举升成本平均下降38.56元/t,年节约能耗168.89万元.

关键词: 辽河油田, 超稠油, 井筒掺活性水降粘工艺, 先导性试验, 经济效益

Abstract: The viscosity reduction technology for ultra-heavy oil in wellbore with electric heating technique can result in higher energy loss.The viscosity reduction technology by blending active water into wellbore was developed.The experiment result shows that the viscosity rate of ultra-heavy oil can greatly reduced using this technology.The automatic demulsification and dewatering characteristics are better.The content of water in purified oil is 3% after automatically settling for 72 hours at 85℃.The content of water in purified oil reduced to 1% after adding demulsifier with a concentration of 0.04% into low-viscosity oil-water emulsifier and automatically settling for 72 hours at 85℃.The pilot test of viscosity reduction technology by blending active water performed in eight ultra-heavy oil wells in Liaohe Oilfield showed that the blending active water technology could substitute the viscosity reduction technology by electric heating.The electric current of pumping unit in the tested oil well was reduced by 10A to 30A,and the viscosity of liquid produced from wellbore was greatly reduced.The sewage reinjection and mixing technology can save much fresh water.The blending active water technology can reduce the lifting cost of oil production and save energy consumption greatly.

Key words: Liaohe Oilfield, ultra-heavy oil, viscosity reduction technology by blending active water into wellbore, pilot test, economic benefit

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