石油学报 ›› 1998, Vol. 19 ›› Issue (4): 104-108.DOI: 10.7623/syxb199804019

• 石油工程 • 上一篇    下一篇

产出液预分离水力旋流器的机理及试验研究

蒋明虎, 赵立新, 贺杰, 李枫   

  1. 大庆石油学院
  • 收稿日期:1997-12-09 出版日期:1998-10-25 发布日期:2013-07-08
  • 作者简介:蒋明虎,i&84年毕业于大庆石油学院,19&9年于燕山大学获硕士学位.现为大庆石油学院机械系副主任,副教授.通讯处:黑龙江省安达市.邮政编码:1514000
  • 基金资助:
    黑龙江省自然科学基金

TEST STUDY (JN HYDRC}CYCLQNE USED FOR PRE-SEPARATING OIL WELL PRCDUCED-WATER

Jiang Minghu   

  1. Daqing Petroleum Institute
  • Received:1997-12-09 Online:1998-10-25 Published:2013-07-08

摘要: 根据油田生产需要,从试验分析出发,提出了水力旋流器的部分结构参数与操作参数之间的几个重要的关系式,进而研制开发了用于高含水油井产出液预分离的水力旋流器.并通过对其流场特性的分析发现,预分离水力旋流器的溢流口直径加大后,为提高预分离效率,必须将溢流管伸入旋流腔一定长度,同时操作参数也应控制合理.以此为依据试制出样机.油田现场试验证明,含水量在85%左右的油井产出液经预分离水力旋流器处理后,其溢流含水量完全可达到小于30%的指标,而底流水中含油也可降至1%左右,基本满足了处理后的水质指标要求,可在油田上推广应用.

关键词: 分离技术, 水力旋流器, 流场, 机理研究, 现场试验, 推广应用

Abstract: In order to meet the needs of production,several important relations among structural and operating parameters of hydrocyclone are attained based on experiment analysis.According to flow field properties,if overflow pipe is extended into the case in some depth,and the operating parameters are reasonable,the pre separation efficiency is promoted with the enlargement of dia meter of overflowing vent.Based on the research,some samples have been developed,and put into field applicaiton.It is found that when the production fluid which contains 85% water is preseparated by operating the samples,the water content in overflowing fluid is less than 30%,and oil content in downflowing water drops about 1%.It reaches the index of quality of processed water These machines can be generalized to field application.

Key words: separation technique, hydrocylone, flowfield mechanism research, field test, popularized application