Editorial office of ACTA PETROLEI SINICA ›› 1998, Vol. 19 ›› Issue (1): 96-99.DOI: 10.7623/syxb199801018

• Petroleum Engineering • Previous Articles     Next Articles

A STUDY ON MECHANISMS AND EFFECTS OF PLUG REMOVAL NEAR WELLBORE WITH HIGH PRESSURE WATER JET

Li Gensheng1   

  1. Petroleum University, Huadong
  • Received:1997-01-29 Online:1998-01-25 Published:2011-03-16

高压水射流处理地层的机理及试验

李根生1, 马加计1, 沈晓明1, 张彦福2, 毕文亮2   

  1. 1. 石油大学 华东;
    2. 辽河石油勘探局
  • 作者简介:李根生,1986年毕业于华东石油学院北京研究生部。现为石油大学(华东)石油工程系教授。通讯处:山东省东营市。邮政编码:257062。
  • 基金资助:
    山东省自然科学基金青年基金

Abstract: The mechanisms of the laboratory and field test results of plug removal near wellbore with high pressure water jet are introduced.A new tool for plug removal by three kinds of compound physical effects of low frequency hydraulic pulse, high frequency oscillating jet impact and cavitation noise are developed.The effects of jet pressure on rotating speed, jet impact pressure and the effects of jet distance on impact pressure are experimentally tested.The experiments have demonstrated that the rotating speed of the tool head and the jet impact pressure on casing surface increase while pump pressure are higher.Jet impact pressure is detectable for large radius of near wellbore formation up to 600 mm at tested pump pressure of 20.0MPa.Field tests at 23 oil wells in Liaohe Oilfield have shown that the plug removal near wellbore with high pressure water jet can increase oil production by 20% to 50%, valid ratio over 90% and the valid period are over 90 days.

Key words: water jet, near wellbore area, plug removal, stimulation effect, stimulation treatment, EOR

摘要: 介绍了高压水射流深穿透处理地层解堵的三种物理机理,即低频旋转水力波、高频振荡射流冲击波和空化噪声超声波。实验室测试了解堵工具的旋转速度特性、冲击压力特性和射流冲击压力随喷距的变化规律。结果表明,随着泵压的增加,解堵工具的旋转速度增大,射流对套管壁面及炮眼冲击力也随之增大。在泵压一定的条件下,随着喷距的增加,射流冲击压力逐渐减弱。在试验的泵压20.0MPa条件下,射流压力作用深度可达600mm以上。经辽河油田23口油井现场试验表明,高压水射流深穿透解堵技术平均单井增油幅度达20%~50%,有效率90%以上,有效期90d以上,是高含水期油田强化生产、增产增注、提高采收率的一种高效新技术。

关键词: 水力射流, 近井地带, 解堵, 增产效果, 增产措施, 采收率